
Predictive Maintenance Case Study: Hydrogen Compressor Failure Prevention
Case study showing how Aspen Mtell predicted hydrogen compressor failure 35 days ahead, enabling planned maintenance and avoiding $75M in losses.
Diversified energy company deployed Aspen Mtell on a critical hydrogen compressor after three prior failures caused over $250M in losses. The solution generated seven anomaly and four failure agents that detected piston, valve, and lubricator issues with 24-38 days advance notice. Planned intervention reduced downtime by up to eight days and delivered 30 percent maintenance cost savings versus emergency repairs.
Aspen Mtell detected compressor failure 35 days before occurrence across piston, valve, and lubricator modes
Planned maintenance achieved 30 percent cost reduction versus emergency repairs
Avoided up to eight days of unplanned downtime through scheduled shutdown windows
Combined production and maintenance savings potential exceeded $75M across three historical events
Rollout expanded to 300+ assets across 12 refineries and 6 pipelines following pilot success